Moderators: jsumali2, richierich, ua900, PanAm_DC10, hOMSaR
planecane wrote:shmerik wrote:The more info that comes out about what Boeing knew about MCAS the less it all makes sense to me. I know this may be seen as hyperbole as some and it's just pure speculation as we don't have access to test flight info, but at this point I wouldn't be surprised if the massive increase in authority came from discovering more extreme behavior on approach to stall than just slight stick lightening.
For the 100th time (and this has been reported in multiple articles), the increase in authority came because they discovered that MCAS was needed in low speed situations when it was originally designed for high speed situations. In the low speed situation, the stabilizer needs to move more in order to create the same force.
Look out the window at the ailerons on your next flight. Shortly after takeoff or when close to landing they deflect a lot and the bank angle barely changes. At cruise, the movement is almost imperceptible but the bank angle changes significantly. It is the exact same reason.
JTAR Final Report wrote:Observation O3.4-B: Extension of MCAS to the low-speed and 1g environment during the flight program WAS DUE TO UNACCEPTABLE STALL CHARACTERISTICS WITH STS ONLY. The possibility of a pitch-up tendency during approach to stall was identified for the flaps-up configuration prior to the implementation of MCAS.
Finding F3.5-C: The JATR team considers that the STS/MCAS and EFS functions could be considered as stall identification systems or stall protection systems, depending on the natural (unaugmented) stall characteristics of the aircraft.
morrisond wrote:PW100 wrote:morrisond wrote:I'll ignore JT for now as neither of us could say for sure what would have happened - we just have our beliefs.
ET is a lot easier though to say they would not have saved an NG with runaway trim either.
After MCAS had activated a few times on ET and they turned off the trim switches they would have been at the same condition as runaway trim on an NG with the Electric trim off - yet they did not save it.
Failure to put the plane back in trim before hitting switches/Failure to control airspeed/ possibly not being familiar with the backup trim system (same as on the NG), manual trim system possibly not working due to excessive speed would have caused them to crash an NG as well - for if they had turned the switches back on an NG the runaway pitch trim would have resumed resulting in putting them in the ground faster as it would have been one continuous pitch change motion.
They would not have saved an NG either.
I'm calling BS.
You are totally ignoring that any crew could fall into this trap as the run-away MCAS was camouflaged by all sort of alerts (like Stick Shaker/Stall Warning/Master Caution Ant-Ice/Unreliable Air Speed), and there was no clue (no EICAS) to help the crew prioritize the Christmas tree light-up they were being presented.
Also, as I have argued before I'm not convinced (at this stage) that leaving the aircraft in untrimmed condition when they hit the switches was by their choice. All four crew up-trim actions (after MCAS run-away) stopped at exactly the same point. Even if you wanted to do that on purpose you probably would not succeed in that.
I'd expect that between 25% and 75% of decently trained western crews would also have crashed, for above mentioned reasons.
So if you were in an NG that had real runaway trim (you would have had to hit both switches to turn off electric trim entirely and stop the runaway) and you are way out of trim over Vmo with AT TOGA engaged possibly making it difficult to use the manual trim wheels (that fact is not established yet) what would you do to recover?
What is the first thing you would do?
sgrow787 wrote:XRAYretired wrote:Another Herculean analysis from Peter Lemme.
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
seahawk wrote:morrisond wrote:dtw2hyd wrote:
Even though the captain was fighting MCAS thru trim switch, it was a losing battle as with every MCAS-ANU iteration MCAS was gaining. At some point, it reached the point of no return.
No the Captain was doing a great Job fulling offsetting MCAS on average 22 times - it's only when the FO took over that the battle was lost - in 2-3 instances of MCAS activation as it seems like he did not know who to use the trim properly and was not told about it by the Captain.
And if you have to trim up 22 times, one can expect a reasonably skilled crew to come up with the runaway trim checklist and disable the system. The crews showed unacceptable bad crew resource management and lacked basic flying skills, which must be seen as the final factors for the crash.
PW100 wrote:morrisond wrote:PW100 wrote:
I'm calling BS.
You are totally ignoring that any crew could fall into this trap as the run-away MCAS was camouflaged by all sort of alerts (like Stick Shaker/Stall Warning/Master Caution Ant-Ice/Unreliable Air Speed), and there was no clue (no EICAS) to help the crew prioritize the Christmas tree light-up they were being presented.
Also, as I have argued before I'm not convinced (at this stage) that leaving the aircraft in untrimmed condition when they hit the switches was by their choice. All four crew up-trim actions (after MCAS run-away) stopped at exactly the same point. Even if you wanted to do that on purpose you probably would not succeed in that.
I'd expect that between 25% and 75% of decently trained western crews would also have crashed, for above mentioned reasons.
So if you were in an NG that had real runaway trim (you would have had to hit both switches to turn off electric trim entirely and stop the runaway) and you are way out of trim over Vmo with AT TOGA engaged possibly making it difficult to use the manual trim wheels (that fact is not established yet) what would you do to recover?
What is the first thing you would do?
You forgot to add Stick Shaker/Stall Warning/Master Caution Ant-Ice/Unreliable Air Speed warnings/alerts. Throw in those factors, and you'd likely crash your NG if you are below FL100, no matter what checklist you pull out.
PW100 wrote:sgrow787 wrote:XRAYretired wrote:Another Herculean analysis from Peter Lemme.
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
PW100 wrote:sgrow787 wrote:XRAYretired wrote:Another Herculean analysis from Peter Lemme.
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
Revelation wrote:DenverTed wrote:Revelation wrote:
It also points out that Forkner is now a WN pilot and member of the SWAPA pilot's union, the same union that is suing Boeing for $100M+ for lost wages, some of which presumably would be paid out to Forkner should they win the law suit. Ironic, eh?
That's some Jedi stuff for sure.
Meanwhile in the US, the news cycle for the CEO hearings has passed, now the impeachment drama has all the eyeballs with no indication whatsoever that the ungrounding timeline has shifted.
morrisond wrote:PW100 wrote:sgrow787 wrote:
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.
PW100 wrote:Revelation wrote:DenverTed wrote:
That's some Jedi stuff for sure.
Meanwhile in the US, the news cycle for the CEO hearings has passed, now the impeachment drama has all the eyeballs with no indication whatsoever that the ungrounding timeline has shifted.
MCAS was initially designed for the high speed winding turn. The part of the flight envelope a crew would normally never be expected to see. This was Forkner’s main justification to have MCAS reference removed from the pilot operating manual (FCOM). Forkner then realized that he had lied (unknowingly) to the FAA, as he was not included in the memo that MCAS was extended to the low speed regime.
What I wanted to hear from Muilenburg is whether Boeing got back to the FAA once they (Forkner, and Gustavsson) realized that they had lied (unknowingly) to the FAA. I mean, lying unknowingly is not that bad, things do change during development and testing phases. But not forwarding the newly gained knowledge, and associated reasons for not mentioning MCAS in the FCOM would be the real bad thing.
morrisond wrote:PW100 wrote:morrisond wrote:
So if you were in an NG that had real runaway trim (you would have had to hit both switches to turn off electric trim entirely and stop the runaway) and you are way out of trim over Vmo with AT TOGA engaged possibly making it difficult to use the manual trim wheels (that fact is not established yet) what would you do to recover?
What is the first thing you would do?
You forgot to add Stick Shaker/Stall Warning/Master Caution Ant-Ice/Unreliable Air Speed warnings/alerts. Throw in those factors, and you'd likely crash your NG if you are below FL100, no matter what checklist you pull out.
So I take it you are retracting you calling BS on me as they would have crashed the NG as well as they didn't actually have a real grasp of how to control the plane without the AP. Just like the Captain of ET409 who crashed an NG while trying to fly manually who went through ET training at about the same time as the ET302 Captain.
BTW - the answer was - disconnect the AT and get control of the airspeed so the manual trim wheel becomes usuable. You would have had to do that on an NG as well.
morrisond wrote:PW100 wrote:Revelation wrote:Meanwhile in the US, the news cycle for the CEO hearings has passed, now the impeachment drama has all the eyeballs with no indication whatsoever that the ungrounding timeline has shifted.
MCAS was initially designed for the high speed winding turn. The part of the flight envelope a crew would normally never be expected to see. This was Forkner’s main justification to have MCAS reference removed from the pilot operating manual (FCOM). Forkner then realized that he had lied (unknowingly) to the FAA, as he was not included in the memo that MCAS was extended to the low speed regime.
What I wanted to hear from Muilenburg is whether Boeing got back to the FAA once they (Forkner, and Gustavsson) realized that they had lied (unknowingly) to the FAA. I mean, lying unknowingly is not that bad, things do change during development and testing phases. But not forwarding the newly gained knowledge, and associated reasons for not mentioning MCAS in the FCOM would be the real bad thing.
As part of his testimony he did say the FAA knew that they had extended it to the low speed regime as well.
morrisond wrote:PW100 wrote:morrisond wrote:
No - it was the First Officer who didn't know how to offset the Yoke forces with electric trim who was pulling with 105 lbs of force - he did not have a stick shaker going off on his side.
Do you seriously think that the FO did not know how to offset yoke forces, never used electrical trim before?
If you really believe that, then I find it easy to understand why your posts continue to focus on how the crew basically crashed the plane.
The KNKT investigators pointed that out. He was cited repeatedly in SIM training for being behind the aircraft and not being able to control it during manual flight.
It wasn't me making that up.
morrisond wrote:PW100 wrote:morrisond wrote:I don't doubt it all - that's why "Global training standards need to improve Worldwide" this is not only a third world training problem. It needs to be fixed with regulation - just like Boeing and the FAA need to be fixed.
Just hopefully on average on the big western airlines the average competency is better and chance doesn't give you a bad crew and the holes in the swiss cheese don't line up when something goes wrong.
“Global training standards Worldwide” are reasonably fine. Could they be improved? Sure. But accident rates have never been better than today, if we leave the Max out of the equation.
The accident rates being lower doesn't necessarily mean the crews are getting better - it just basically means the systems are getting better and there are having less catastrophic failures and instances where Pilots are having to show they know what they are doing is fewer than ever thankfully.
PW100 wrote:morrisond wrote:PW100 wrote:
You forgot to add Stick Shaker/Stall Warning/Master Caution Ant-Ice/Unreliable Air Speed warnings/alerts. Throw in those factors, and you'd likely crash your NG if you are below FL100, no matter what checklist you pull out.
So I take it you are retracting you calling BS on me as they would have crashed the NG as well as they didn't actually have a real grasp of how to control the plane without the AP. Just like the Captain of ET409 who crashed an NG while trying to fly manually who went through ET training at about the same time as the ET302 Captain.
BTW - the answer was - disconnect the AT and get control of the airspeed so the manual trim wheel becomes usuable. You would have had to do that on an NG as well.
ET speed was OK right up until MCAS run-away. If run-away trim would hit NG at that very same point, the result would not have been different. No matter what crew.
asdf wrote:Northpole wrote:I read somewhere in Swedish newspaper that Kevin McAllister has been sacked from Boeing
seems like ...
https://www.streetinsider.com/Corporate ... 34229.html
Boeing (BA) Announces Stan Deal to Succeed Kevin McAllister as CEO of Boeing Commercial Airplanes
shmerik wrote:Actually the more I look at the graphs the more confused I'm getting. It looks like they were having more success at climbing even as MCAS was trimming down than after shutting off stab trim.
Compare the pitch attitude display from 05:41:00 - 05:41:15 shortly after flipping the switches to from 05:41:15 - 05:43:15. Looks like things were pretty stable and then there was a loss of control around 05:41:15, is this because of too much speed or what?
Any ideas?
XRAYretired wrote:shmerik wrote:Actually the more I look at the graphs the more confused I'm getting. It looks like they were having more success at climbing even as MCAS was trimming down than after shutting off stab trim.
Compare the pitch attitude display from 05:41:00 - 05:41:15 shortly after flipping the switches to from 05:41:15 - 05:43:15. Looks like things were pretty stable and then there was a loss of control around 05:41:15, is this because of too much speed or what?
Any ideas?
https://www.satcom.guru/2019/04/what-ha ... et302.html
Have a look at some detailed analysis.
Ray
StTim wrote:Do you know what - I actually don't care if the crew could have saved the plane. They should never have been put in that position. End of - period.
This saga started with terrible design and ended with pilots fighting for their - and their passengers lives.
I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
sgrow787 wrote:planecane wrote:For the 100th time (and this has been reported in multiple articles), the increase in authority came because they discovered that MCAS was needed in low speed situations ...
But common sense says they would have maintained the high-speed authority at 0.6 deg/cyc. In fact, it may be the case that they failed to keep that in the design, or they kept it in the design, but failed to implement it correctly, although we know they implemented it correctly with MCAS 0.0 G+AOA design, so that argument doesn't hold water.
I don't recall the timeline that they became aware of the low-speed issue and MCAS solution/authority change. If it was early enough before certification (more than a year I would think), then it's hard to argue they ran out of time to get that one right, leading one to believe they didn't want the new solution to veer far from the 0.6 deg/cyc version they submitted previously to the FAA (ie, let's just change the number rather than have a new paragraph explaining the logic behind an authority change - if airspeed indicates low speed, use 2.5, if high speed, use 0.6).
Chemist wrote:StTim wrote:Do you know what - I actually don't care if the crew could have saved the plane. They should never have been put in that position. End of - period.
This saga started with terrible design and ended with pilots fighting for their - and their passengers lives.
I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
I agree with your statements. But do you really think an FO that doesn't use trim and can't find checklists they are supposed to have memorized is reasonably well trained?
PW100 wrote:sgrow787 wrote:XRAYretired wrote:Another Herculean analysis from Peter Lemme.
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
PW100 wrote:morrisond wrote:PW100 wrote:
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.
So we now have conflicting, opposing info how a decently trained pilot should handle the trim at high speed. Great. Carry on throwing the crew under the bus.
StTim wrote:Do you know what - I actually don't care if the crew could have saved the plane. They should never have been put in that position. End of - period.
This saga started with terrible design and ended with pilots fighting for their - and their passengers lives.
I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
shmerik wrote:XRAYretired wrote:shmerik wrote:Actually the more I look at the graphs the more confused I'm getting. It looks like they were having more success at climbing even as MCAS was trimming down than after shutting off stab trim.
Compare the pitch attitude display from 05:41:00 - 05:41:15 shortly after flipping the switches to from 05:41:15 - 05:43:15. Looks like things were pretty stable and then there was a loss of control around 05:41:15, is this because of too much speed or what?
Any ideas?
https://www.satcom.guru/2019/04/what-ha ... et302.html
Have a look at some detailed analysis.
Ray
Thanks, so it seems that at that point they must have been exerting themselves significantly to keep the nose up
morrisond wrote:
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.
ikramerica wrote:Another question I have is about the previous flight. Were the two pilots known as exceptional? Did they always pass all their training at 100% perfection? Did the report get into their history at all? We know the FO of the final flight was deficient but somehow allowed to be in the seat, but what of the previous crew that figured it out and hand flew the plane safely to the destination?
dtw2hyd wrote:morrisond wrote:
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.
Have you read the report? FO used ANU trim six times.
23:30:48 - Captain asked FO to take control (Pitch Trim 4.8)
23:30:49 - FO ANU trim for 3 seconds
23:30:52 - FO - I have control
23:31:00 - Automatic trim for 8 seconds (Pitch Trim from 5.4 to 3.4)
23:31:08 - FO - ANU trim for 1 second (Pitch 3.5)
23:31:15 - MCAS for 3 seconds
23:31:17 - FO - ANU trim for 1 second (Pitch 2.9, back pressure 65 lbs)
23:31:19 - FO - ANU trim for 4 seconds (Pitch 3.4)
23:31:27 - MCAS for 8 seconds (Pitch 1.8, back pressure 82 lbs)
23:31:37 - FO - ANU trim for 2 seconds (Pitch 1.3)
23:31:43 - MCAS for 4 seconds (Pitch 0.3, back pressure 93 lbs)
23:31:46 - FO - ANU trim for 2 seconds (Captain PFD 3200ft, FO PFD 3600ft, rate of descent 10,000 ft/sec)
23:31:51 - TERRAIN and SINK RATE warnings
23:31:53 - MCAS activated until recording stopped. This must be a proud moment for the software team.
dtw2hyd wrote:morrisond wrote:
23:31:19 - FO - ANU trim for 4 seconds (Pitch 3.4)
23:31:27 - MCAS for 8 seconds (Pitch 1.8, back pressure 82 lbs)
23:31:37 - FO - ANU trim for 2 seconds (Pitch 1.3)
23:31:43 - MCAS for 4 seconds (Pitch 0.3, back pressure 93 lbs).
StTim wrote:Chemist wrote:StTim wrote:Do you know what - I actually don't care if the crew could have saved the plane. They should never have been put in that position. End of - period.
This saga started with terrible design and ended with pilots fighting for their - and their passengers lives.
I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
I agree with your statements. But do you really think an FO that doesn't use trim and can't find checklists they are supposed to have memorized is reasonably well trained?
But remember there was only a but of differences training for the crews who flew the MAX over the NG and in the AoA setting off the MCAS they were in uncharted territory that they had not been trained for.
dtw2hyd wrote:What good was Airspeed Unreliable checklist? Was it even the correct checklist for the problem as manifested?
seahawk wrote:And if you have to trim up 22 times, one can expect a reasonably skilled crew to come up with the runaway trim checklist and disable the system. The crews showed unacceptable bad crew resource management and lacked basic flying skills, which must be seen as the final factors for the crash.
morrisond wrote:The accident rates being lower doesn't necessarily mean the crews are getting better
Chemist wrote:But do you really think an FO that doesn't use trim and can't find checklists they are supposed to have memorized is reasonably well trained?
morrisond wrote:StTim wrote:I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
You need to read the JT crash final report - they were not even close to average in terms of ability.
morrisond wrote:dtw2hyd wrote:morrisond wrote:
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.
Have you read the report? FO used ANU trim six times.
23:30:48 - Captain asked FO to take control (Pitch Trim 4.8)
23:30:49 - FO ANU trim for 3 seconds
23:30:52 - FO - I have control
23:31:00 - Automatic trim for 8 seconds (Pitch Trim from 5.4 to 3.4)
23:31:08 - FO - ANU trim for 1 second (Pitch 3.5)
23:31:15 - MCAS for 3 seconds
23:31:17 - FO - ANU trim for 1 second (Pitch 2.9, back pressure 65 lbs)
23:31:19 - FO - ANU trim for 4 seconds (Pitch 3.4)
23:31:27 - MCAS for 8 seconds (Pitch 1.8, back pressure 82 lbs)
23:31:37 - FO - ANU trim for 2 seconds (Pitch 1.3)
23:31:43 - MCAS for 4 seconds (Pitch 0.3, back pressure 93 lbs)
23:31:46 - FO - ANU trim for 2 seconds (Captain PFD 3200ft, FO PFD 3600ft, rate of descent 10,000 ft/sec)
23:31:51 - TERRAIN and SINK RATE warnings
23:31:53 - MCAS activated until recording stopped. This must be a proud moment for the software team.
Yes I did and he never did it for long enough - what is your point?
morrisond wrote:Yes I did and he never did it for long enough - what is your point?
rheinwaldner wrote:seahawk wrote:And if you have to trim up 22 times, one can expect a reasonably skilled crew to come up with the runaway trim checklist and disable the system. The crews showed unacceptable bad crew resource management and lacked basic flying skills, which must be seen as the final factors for the crash.
Trimming happens as you steer your car. You are not really aware of the corrections and dont notice the directions and dont count the inputs. And as small stick forces were continuously canceled out, the corrections were small and it felt naturally. There was no clue from the system, that the small mistrims that occured 26 times were coming froming a hidden trim system itself. And the frequent small corrections masked the brutally long cycle, MCAS would have ran otherwise.
Please also consider, that the accident report does not nearly put weight on the crew errors that you do. In other words, you are making stuff up.
rheinwaldner wrote:morrisond wrote:StTim wrote:I don't planes that need the creme de la creme to fly them. I want planes that the average pilot, reasonably well trained can fly safely. That seems to be about every other plane bar the MAX!
You need to read the JT crash final report - they were not even close to average in terms of ability.
Yes, read it! And stick with the findings of it rather than spinning your own version of it. Try to read the rest of the report instead of the few pages, that you quoted so far. Then you see, that StTim was right.
rheinwaldner wrote:morrisond wrote:dtw2hyd wrote:
Have you read the report? FO used ANU trim six times.
23:30:48 - Captain asked FO to take control (Pitch Trim 4.8)
23:30:49 - FO ANU trim for 3 seconds
23:30:52 - FO - I have control
23:31:00 - Automatic trim for 8 seconds (Pitch Trim from 5.4 to 3.4)
23:31:08 - FO - ANU trim for 1 second (Pitch 3.5)
23:31:15 - MCAS for 3 seconds
23:31:17 - FO - ANU trim for 1 second (Pitch 2.9, back pressure 65 lbs)
23:31:19 - FO - ANU trim for 4 seconds (Pitch 3.4)
23:31:27 - MCAS for 8 seconds (Pitch 1.8, back pressure 82 lbs)
23:31:37 - FO - ANU trim for 2 seconds (Pitch 1.3)
23:31:43 - MCAS for 4 seconds (Pitch 0.3, back pressure 93 lbs)
23:31:46 - FO - ANU trim for 2 seconds (Captain PFD 3200ft, FO PFD 3600ft, rate of descent 10,000 ft/sec)
23:31:51 - TERRAIN and SINK RATE warnings
23:31:53 - MCAS activated until recording stopped. This must be a proud moment for the software team.
Yes I did and he never did it for long enough - what is your point?
That you were wrong, saying the FO did not trim at all.
seahawk wrote:Any decent pilot should be able to notice when the plane is trimmed neutral and should trim accordingly.
oschkosch wrote:AA news! Sounds like it is getting more difficult!
https://www.reuters.com/article/us-boei ... SKBN1XA2JO
American Airlines’ flight attendants union still has safety concerns about the Boeing 737 MAX and is demanding an active role in the relaunch of the grounded aircraft, its president told Boeing Co’s (BA.N) chief executive in a letter seen by Reuters.
“The 28,000 flight attendants working for American Airlines refuse to walk onto a plane that may not be safe and are calling for the highest possible safety standards to avoid another tragedy,” Association of Professional Flight Attendants President Lori Bassani said in the letter.
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planecane wrote:oschkosch wrote:AA news! Sounds like it is getting more difficult!
https://www.reuters.com/article/us-boei ... SKBN1XA2JO
American Airlines’ flight attendants union still has safety concerns about the Boeing 737 MAX and is demanding an active role in the relaunch of the grounded aircraft, its president told Boeing Co’s (BA.N) chief executive in a letter seen by Reuters.
“The 28,000 flight attendants working for American Airlines refuse to walk onto a plane that may not be safe and are calling for the highest possible safety standards to avoid another tragedy,” Association of Professional Flight Attendants President Lori Bassani said in the letter.
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What expertise do FAs have here? If the PILOTS agree that it is safe to fly then the FAs shouldn't have an issue. The pilots make that call on every flight every day. Should the FAs have a say every flight? I don't think so.
mjoelnir wrote:planecane wrote:oschkosch wrote:AA news! Sounds like it is getting more difficult!
https://www.reuters.com/article/us-boei ... SKBN1XA2JO
American Airlines’ flight attendants union still has safety concerns about the Boeing 737 MAX and is demanding an active role in the relaunch of the grounded aircraft, its president told Boeing Co’s (BA.N) chief executive in a letter seen by Reuters.
“The 28,000 flight attendants working for American Airlines refuse to walk onto a plane that may not be safe and are calling for the highest possible safety standards to avoid another tragedy,” Association of Professional Flight Attendants President Lori Bassani said in the letter.
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What expertise do FAs have here? If the PILOTS agree that it is safe to fly then the FAs shouldn't have an issue. The pilots make that call on every flight every day. Should the FAs have a say every flight? I don't think so.
We have seen the expertise of the test pilots at Boeing when judging the safety of the 737MAX. Dismal results.
seahawk wrote:As I previously said the crew performance and the design error are not directly connected.
Just if you look at the trim inputs, it becomes obvious that without coming to the conclusion that it is a runaway trim, they could not win the struggle. In 10 seconds MCAS trimmed from 6,1 units to 3,8 units, while 5 seconds of manual trim only set the trim back to 4,7 units. So MCAS did trim for 0,23 units per second, while manual electric trim only trims for 0,18 units per second.
But we also see the the pilot used manul inputs to stop the MCAS quickly and was able to control the trim quite well. The FO re-acted slower and counter trimmed less. When handing over control the pilot failed to inform the FO of the constant need to counter a trim movement manually. That is bad crew management.
It does not make the mistakes by Boeing any better.
morrisond wrote:seahawk wrote:Any decent pilot should be able to notice when the plane is trimmed neutral and should trim accordingly.
Any pilot who successfully completes the first few hours of basic training should be able to do that - it should be a reflex reaction within the the first 20-30 hours.
It's incomprehensible how someone with that much experience didn't know how to trim correctly.
planecane wrote:mjoelnir wrote:planecane wrote:What expertise do FAs have here? If the PILOTS agree that it is safe to fly then the FAs shouldn't have an issue. The pilots make that call on every flight every day. Should the FAs have a say every flight? I don't think so.
We have seen the expertise of the test pilots at Boeing when judging the safety of the 737MAX. Dismal results.
I'm talking about the AA pilots who put their lives on the aircraft and who now have all information about the MAX and MCAS. They have the expertise to understand the aircraft and the changes made. FAs do not have the education and expertise to determine the safety of the MAX.
planecane wrote:seahawk wrote:As I previously said the crew performance and the design error are not directly connected.
Just if you look at the trim inputs, it becomes obvious that without coming to the conclusion that it is a runaway trim, they could not win the struggle. In 10 seconds MCAS trimmed from 6,1 units to 3,8 units, while 5 seconds of manual trim only set the trim back to 4,7 units. So MCAS did trim for 0,23 units per second, while manual electric trim only trims for 0,18 units per second.
But we also see the the pilot used manul inputs to stop the MCAS quickly and was able to control the trim quite well. The FO re-acted slower and counter trimmed less. When handing over control the pilot failed to inform the FO of the constant need to counter a trim movement manually. That is bad crew management.
It does not make the mistakes by Boeing any better.
They could have won the struggle. If, each time, they trimmed back to neutral column force (like is supposed to be done as part of normal manual flight) then they would have just kept oscillating back and forth between neutral and 2.5 units out of trim nose down until they set flaps 1 in preparation for landing. It doesn't matter if it took them longer to offset MCAS than it took MCAS to reach a particular point. Trim is not done by time, it is done by feel.
morrisond wrote:PW100 wrote:sgrow787 wrote:
"Observation O6.9-H: Boeing concluded that multiple erroneous MCAS activations were not worse than a single erroneous activation, based on the assumption that the crew would return the aircraft to a trimmed state (consistent with AC 25-7C guidance) following each activation."
It would seem to me, a non-pilot, that the increase in airspeed that comes with MCAS AND action, would result in the pilot needing less pitch correction to return to stable flight. Would this explain the lack of return of the stab trim all the way to what it was pre-AND?
BTW, from what I can tell from the DFDR plots, the authority from the eTrim is only 0.15 deg/sec, which is about 40% less than the 0.27 deg/sec (2.5 [deg/cyc] / 9 [sec/cyc]) from MCAS, which is significant.
Also, in one of the earlier threads, we were told that any decently trained pilot would not put in electric trimming in one loooong go, especially at higher speeds, but in short blips. Then evaluating the effect, and if needed, put in another short burst. But during the evaluation, MCAS run-away becomes alive again, and aggressively trims the nose down, at much higher rate than electric up-trimming could do at that point.
A decently trained pilot would have realized they were way out of trim and held that switch down until the forces were neutralized - just like the JT Captain did - he actually didn't do too bad - just never made the intuitive leap to turn off the system after 22 times - maybe 23 times would have done it - before turning it over to this FO and forgetting to tell him what he had to do to offset what MCAS was doing to the plane.
Maybe it was so obvious that he assumed he didn't have to tell him but that was really CRM.